書誌事項
- タイトル別名
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- EFFECT OF SUCTION REDUCTION CAUSED BY WETTING PROCESS ON SHEAR STRENGTH CHARACTERISTICS UNER LOW CONFINING PRESSURE
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抄録
In this study, triaxial compression test under low confining pressure and undrained state were carried out for saturated and unsaturated kaoline specimens and undisturbed sample, to study the effect of suction reduction caused by wetting process, and effective stress path shear and strength characteristics were examined. From the test results, it was found that the intergranular adhesive force between soil particles affects on the peak strength, and that the residual strengths were arranged uniquely for the effective mean stress taking the suction stress as confining pressure. And we proposed one prediction method for the strength reduction caused by decrease of suction during wetting process.
収録刊行物
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- 土木学会論文集C
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土木学会論文集C 62 (2), 471-487, 2006
公益社団法人 土木学会
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詳細情報 詳細情報について
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- CRID
- 1390282680231375872
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- NII論文ID
- 10019322084
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- NII書誌ID
- AA12131726
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- ISSN
- 1880604X
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- データソース種別
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- JaLC
- Crossref
- CiNii Articles
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- 抄録ライセンスフラグ
- 使用不可